Ray Barnes
Well-Known Member
- Joined
- Aug 30, 2006
- Messages
- 137
Well...Josh Stollfuss met me at the Ford pond on Saturday. I had a great time, even though the boat didn't get full lap. Before I had gotten to the pond I had lowered the strut a little and put on a 1460 to see if it would be any different from last Thursday. It did help a little and the boat went out about 12' (a new record) then the nose dove and she stalled. The engine fired right up and didn't have anymore problems with it running. I believe the problem was that the carb had come loose Thursday and was sucking air. Next we tried adjusting the angel of the strut. That didn't do much but we did get out a couple of more feet. It kept leaning to the right side and the nose would dive and she pull in water. I had allot of practice retrieving that boat, and man are the heavy and hard to lift when they are full of water. I decided to pull the strut down as far as it would go and added a 457 3 blade. We fired it up and headed for the launch it went out and was trying to get up but didn't want to pop off the surface...so I got a little ticked and just pulled back on the throttle and she broke free and took of like a rocket.
It caught me by suprise and I was a little shakey with the steering, took it on the back straight away and she was stuck nice and haulin. I then realized that I was to far out and tried to bring it in closer to the course and did some havic on the corner bouye. She kept going and started making some wierd popping noise and stalled. Brought it back in and the pipe had slide out of the coupler and caused it to stall. I didn't get many runs in but I was happy to know that the changes I had made wern't the problem and it's just a matter of time before I get it figured out. I'm going to add some more room for adjustment on the strut and make some changes to tightening things down.
I would like to thank Josh for spending the time to help me get it running. He made the day a great exsperience aside form the little set backs on the boat. Looking forward to my next visit. Thanks
It caught me by suprise and I was a little shakey with the steering, took it on the back straight away and she was stuck nice and haulin. I then realized that I was to far out and tried to bring it in closer to the course and did some havic on the corner bouye. She kept going and started making some wierd popping noise and stalled. Brought it back in and the pipe had slide out of the coupler and caused it to stall. I didn't get many runs in but I was happy to know that the changes I had made wern't the problem and it's just a matter of time before I get it figured out. I'm going to add some more room for adjustment on the strut and make some changes to tightening things down.
I would like to thank Josh for spending the time to help me get it running. He made the day a great exsperience aside form the little set backs on the boat. Looking forward to my next visit. Thanks
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